| Commit message (Collapse) | Author | Age | Lines |
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Set the MQ Read Passing & MCIF Cycle limits to the recommended by AMCC
values. This fixes the occasional 440SPe hard locking issues when the 440SPe's
dedicated DMA engines are used (e.g. by the h/w accelerated RAID driver).
Previously the appropriate initialization had been made in Linux, by the
ppc440spe ADMA driver, which is wrong because modifying the MQ configuration
registers after normal operation has begun is not supported and could
have unpredictable results.
Comment from Stefan: This patch doesn't change the resulting value of the
MQ registers. It explicitly sets/clears all bits to the desired state which
better documents the resulting register value instead of relying on pre-set
default values.
Signed-off-by: Yuri Tikhonov <yur@emcraft.com>
Signed-off-by: Stefan Roese <sr@denx.de>
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Reference manual states that MxMR[MAD] increment is the indication
of write to UPM array is complete. Honour that. Also, make the dummy
write explicit.
also fix the comment.
Signed-off-by: Selvamuthukumar <selva.muthukumar@e-coninfotech.com>
Signed-off-by: Kim Phillips <kim.phillips@freescale.com>
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This is needed in unlock_ram_in_cache() because it is called from C and
will corrupt the small data area anchor that is kept in R2.
lock_ram_in_cache() is modified similarly as good coding practice, but
is not called from C.
Signed-off-by: Nick Spence <nick.spence@freescale.com>
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For some reason we duplicated the majority of code in lib_ppc/interrupts.c
Not know how that happened, but there is no good reason for it.
Use the interrupt_init_cpu() and timer_interrupt_cpu() since its why
they exist.
Signed-off-by: Kumar Gala <galak@kernel.crashing.org>
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Switch to the standard CFG_HZ=1000 value, while at it, minor white-space
cleanup, remove CFG_CLKS_IN_HZ from config-headers. Tested on mx31ads,
provides 2% or 0.4% precision depending on the
CONFIG_MX31_TIMER_HIGH_PRECISION flag. Measured with stop-watch on 100s
boot-delay.
Signed-off-by: Guennadi Liakhovetski <lg@denx.de>
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Measurements with our MPC8544 board showed that the I2C bus frequency
is wrong by a factor of 1.5. Obviously, the interpretation of the
MPC85xx_PORDEVSR2_SEC_CFG bit of the cfg_sec_freq register is not
correct. There seems to be an error in the 8544 RM.
Signed-off-by: Wolfgang Grandegger <wg@grandegger.com>
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On 8536DS board, When the DDR clk is set async mode(SW3[6:8] != 111),
The display is still sync mode DDR freq. This patch try to fix
this. The display DDR freq is now the actual freq in both
sync and async mode.
Signed-off-by: Jason Jin <Jason.jin@freescale.com>
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ePAPR says if the *cache-block-size is the same as *cache-line-size
than we don't need the *cache-line-size property.
Signed-off-by: Kumar Gala <galak@kernel.crashing.org>
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The spd_dram code shifts the base address, then masks 20 bits, but
forgets to shift the base address back. Fix this by just masking the
base address correctly.
Found this bug while trying to relocate a DDR memory at the base != 0.
Signed-off-by: Anton Vorontsov <avorontsov@ru.mvista.com>
Signed-off-by: Kim Phillips <kim.phillips@freescale.com>
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After changing SDRAM_CLKTR phase value rerun the memory preload
initialization sequence (INITPLR) to reset and relock the memory
DLL. Changing the SDRAM_CLKTR memory clock phase coarse timing
adjustment effects the phase relationship of the internal, to the
PPC chip, and external, to the PPC chip, versions of MEMCLK_OUT.
Signed-off-by: Adam Graham <agraham@amcc.com>
Signed-off-by: Victor Gallardo <vgallardo@amcc.com>
Signed-off-by: Stefan Roese <sr@denx.de>
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eventually leads to a machine check. This change assures that DPRAM
is allocated only once in that case.
Signed-off-by: Gary Jennejohn <garyj@denx.de>
Signed-off-by: Wolfgang Denk <wd@denx.de>
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Add support watchdog for SH4A core (SH7763, SH7780 and SH7785).
And fix some compile warning.
Signed-off-by: Nobuhiro Iwamatsu <iwamatsu@nigauri.org>
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Signed-off-by: Wolfgang Denk <wd@denx.de>
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Based on original patch by Bernard Blackham <bernard@largestprime.net>
U-boot's HW ECC support for large page NAND on Davinci is completely
broken. Some kernels, such as the 2.6.10 one supported by
MontaVista for DaVinci, rely upon this broken behaviour as they
share the same code for ECCs. In the existing scheme, error
detection *might* work on large page, but error correction
definitely does not. Small page ECC correction works, but the
format is not compatible with the mainline git kernel.
This patch adds ECC code that matches what is currently in the
Davinci git repository (since NAND support was added in 2.6.24).
This makes the ECC and OOB layout written by u-boot compatible with
Linux for both small page and large page devices and fixes ECC
correction for large page devices.
The old behaviour can be restored by defining the macro
CFG_DAVINCI_BROKEN_ECC, which is undefined by default.
Signed-off-by: Hugo Villeneuve <hugo.villeneuve@lyrtech.com>
Acked-by: Sergey Kubushyn <ksi@koi8.net>
Signed-off-by: Scott Wood <scottwood@freescale.com>
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Signed-off-by: Jean-Christophe PLAGNIOL-VILLARD <plagnioj@jcrosoft.com>
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Signed-off-by: Jean-Christophe PLAGNIOL-VILLARD <plagnioj@jcrosoft.com>
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This patch fixes a problem introdiced with patch
bbeff30c [ppc4xx: Remove superfluous dram_init() call or replace it by
initdram()].
The boards affected are:
- PCI405
- PPChameleonEVB
- quad100hd
- taihu
- zeus
Signed-off-by: Stefan Roese <sr@denx.de>
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This patch prevents linker error on AT91RM9200 boards, if
CONFIG_CMD_I2_TREE is set.
It implements i2c_set_bus_speed and i2c_get_bus_speed as a dummy function.
Signed-off-by: Jens Scharsig <esw@bus-elektronik.de>
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ARM DaVinci: Remove duplicate code in cpu/arm926ejs/davinci/dp83848.c
Signed-off-by: Hugo Villeneuve <hugo.villeneuve@lyrtech.com>
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This patch changes get_timer() for i.MX to return the time since
'base' instead of the time since the counter was at zero.
Symptom seen is flash timeout errors when erasing or programming a
sector using the common cfi flash code.
Signed-off-by: Andrew Dyer <adyer@righthandtech.com>
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1) Change the i.MX serial driver to use the baud rate set in the
u-boot environment
2) don't assume a 16MHz value for PERCLK1 in baud rate calculations
3) don't write a 1 to the RDR bit in the USR2 reg. (bit is not "write
one to clear" like other status bits in the reg.)
Signed-off-by: Andrew Dyer <adyer@righthandtech.com>
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Code in cpu/arm920t/start.S will die with a compilation error if
CONFIG_STACKSIZE + CFG_MALLOC_LEN works out to an invalid constant for
the ARM sub instruction. Change the code so that each is subtracted
independently to avoid the error.
Signed-off-by: Andrew Dyer <adyer@righthandtech.com>
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Signed-off-by: Adrian Filipi <adrian.filipi@eurotech.com>
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This patch adds the reset_timer() function (needed by nand_base.c) and
modifies the get_timer_masked() to work in the same way as the omap24xx
function.
Signed-off-by: Magnus Lilja <lilja.magnus@gmail.com>
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Fix printf format-string/arg mismatches under -DDEBUG.
These warnings occur with DEBUG defined for a platform using
cpu/mpc85xx. Users of other architectures can unearth similar
problems by adding the line "CFLAGS += -DDEBUG=1" in config.mk right
after "CFLAGS += $(call cc-option,-fno-stack-protector)".
Signed-off-by: Andrew Klossner <andrew@cesa.opbu.xerox.com>
Signed-off-by: Andy Fleming <afleming@freescale.com>
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The e500um says the timebase is volatile out of reset. To ensure
TB sync works we need to make sure its zero.
Signed-off-by: Kumar Gala <galak@kernel.crashing.org>
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Signed-off-by: Sergei Poselenov <sposelenov@emcraft.com>
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Conflicts:
Makefile
Signed-off-by: Wolfgang Denk <wd@denx.de>
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Since this define is only used on one board that was never really in
production, removing this compile time option doesn't hurt and makes
the code more readable.
Signed-off-by: Stefan Roese <sr@denx.de>
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This patch fixes a compilation warning for the PIP405 board. It moves the
#ifndef CONFIG_CS8952_PHY define a little so that the warning doesn't
occur anymore. I am a little unsure if this #ifdef is at the correct
place now or if it could be removed completely. This needs to get
tested on the PIP405 board.
Signed-off-by: Stefan Roese <sr@denx.de>
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Signed-off-by: Stefan Roese <sr@denx.de>
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This patch adds GPCS, SGMII and M88E1112 PHY support
for the AMCC PPC460GT/EX processors.
Signed-off-by: Victor Gallardo <vgallardo@amcc.com>
Signed-off-by: Stefan Roese <sr@denx.de>
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Signed-off-by: Adam Graham <agraham@amcc.com>
Signed-off-by: Stefan Roese <sr@denx.de>
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Alternate SDRAM DDR autocalibration routine that can be generically used
for any PPC4xx chips that have the IBM SDRAM Controller core allowing for
support of more DIMM/memory chip vendors and gets the DDR autocalibration
values which give the best read latency performance (SDRAM0_RDCC.[RDSS]).
Two alternate SDRAM DDR autocalibration algoritm are provided in this patch,
"Method_A" and "Method_B". DDR autocalibration Method_A scans the full range
of possible PPC4xx SDRAM Controller DDR autocalibration values and takes a
lot longer to run than Method_B. Method_B executes in the same amount of time
as the currently existing DDR autocalibration routine, i.e. 1 second or so.
Normally Method_B is used and it is set as the default method.
The current U-Boot PPC4xx DDR autocalibration code calibrates the IBM SDRAM
Controller registers.[bit-field]:
1) SDRAM0_RQDC.[RQFD]
2) SDRAM0_RFDC.[RFFD]
This alternate PPC4xx DDR autocalibration code calibrates the following
IBM SDRAM Controller registers.[bit-field]:
1) SDRAM0_WRDTR.[WDTR]
2) SDRAM0_CLKTR.[CKTR]
3) SDRAM0_RQDC.[RQFD]
4) SDRAM0_RFDC.[RFFD]
and will also use the calibrated settings of the above four registers that
produce the best "Read Sample Cycle Select" value in the SDRAM0_RDCC.[RDSS]
register.[bit-field].
Signed-off-by: Adam Graham <agraham@amcc.com>
Signed-off-by: Stefan Roese <sr@denx.de>
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This patch fixes warnings like this:
start.S:0: warning: target CPU does not support interworking
which come from some ARM cross compilers and are caused by hard-coded
(with "--with-cpu=arm9" configuration option) ARM targets (which
support ARM Thumb instructions), while the ARM target selected from
the command line (with "-march=armv4") doesn't support Thumb
instructions.
This warning is issued by the compiler regardless of the real use of
the Thumb instructions in code.
To fix this problem, we use options according to compiler version
being used.
Signed-off-by: Sergei Poselenov <sposelenov@emcraft.com>
Signed-off-by: Wolfgang Denk <wd@denx.de>
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Signed-off-by: Sergei Poselenov <sposelenov@emcraft.com>
Signed-off-by: Wolfgang Denk <wd@denx.de>
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ctrl_regs.c: In function 'compute_fsl_memctl_config_regs':
ctrl_regs.c:523: warning: 'caslat' may be used uninitialized in this function
ctrl_regs.c:523: note: 'caslat' was declared here
Add a warning in DDR1 case if cas_latency isn't a value we know about.
Signed-off-by: Kumar Gala <galak@kernel.crashing.org>
Acked-by: Jean-Christophe PLAGNIOL-VILLARD <plagnioj@jcrosoft.com>
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Signed-off-by: Jean-Christophe PLAGNIOL-VILLARD <plagnioj@jcrosoft.com>
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Cleans up some latent issues with the data cache control so that
dcache_enable() and dcache_disable() will work reliably (after
unlock_ram_in_cache() has been called)
Signed-off-by: Nick Spence <nick.spence@freescale.com>
Signed-off-by: Kim Phillips <kim.phillips@freescale.com>
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Record the Arbiter Event Register values and optionally display them.
The Arbiter Event Register can record the type and effective address of
an arbiter error, even through an HRESET. This patch stores the values in
the global data structure.
Display of the Arbiter Event registers immediately after the RSR value
can be enabled with defines. The Arbiter values will only be displayed
if an arbiter event has occured since the last Power On Reset, and either
of the following defines exist:
#define CONFIG_DISPLAY_AER_BRIEF - display only the arbiter address and
and type register values
#define CONFIG_DISPLAY_AER_FULL - display and interpret the arbiter
event register values
Address Only transactions are one of the trapped events that can register
as an arbiter event. They occur with some cache manipulation instructions
if the HID0_ABE (Address Broadcast Enable) is set and the memory region
has the MEMORY_COHERENCE WIMG bit set. Setting:
#define CONFIG_MASK_AER_AO - prevents the arbiter from recording address
only events, so that it can still capture
other real problems.
Signed-off-by: Nick Spence <nick.spence@freescale.com>
Signed-off-by: Kim Phillips <kim.phillips@freescale.com>
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This is needed in unlock_ram_in_cache() because it is called from C and
will corrupt the small data area anchor that is kept in R2.
lock_ram_in_cache() is modified similarly as good coding practice, but
is not called from C.
Signed-off-by: Nick Spence <nick.spence@freescale.com>
Signed-off-by: Kim Phillips <kim.phillips@freescale.com>
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Set DAT value before DIR values to avoid creating glitches on the
GPIO signals.
Set gpio level register before direction register to inhibit
glitches on high level output pins.
Dir and data gets cleared at powerup, so high level output lines see
a short low pulse between setting the direction and level registers.
Issue was seen on a new board with the nReset line of the NOR flash
connected to a GPIO. Setting the direction register puts the NOR flash
in reset so the next instruction to set the level cannot get executed.
Signed-off-by: Nick Spence <nick.spence@freescale.com>
Signed-off-by: Peter Korsgaard <jacmet@sunsite.dk>
Signed-off-by: Kim Phillips <kim.phillips@freescale.com>
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