| Commit message (Collapse) | Author | Age | Lines |
... | |
|\ |
|
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| | |
'sf command' should receive the length in sector boundaries, so fix it
accordingly.
Also, show the steps to set the server and board IP addresses for
making the steps clearer.
Signed-off-by: Otavio Salvador <otavio@ossystems.com.br>
Reviewed-by: Fabio Estevam <fabio.estevam@nxp.com>
|
| |
| |
| |
| |
| |
| |
| |
| |
| | |
We currently support various versions of Solidrun mx6 boards, so
remove the obsolete comment.
Reported-by: Jon Nettleton <jon.nettleton@gmail.com>
Signed-off-by: Fabio Estevam <fabio.estevam@nxp.com>
Reviewed-by: Stefano Babic <sbabic@denx.de>
|
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| | |
Since commit 59370f3fcd1350 ("net: phy: delay only if reset handler is
registered") Ethernet is no longer functional:
Booting from net ...
FEC Waiting for PHY auto negotiation to complete......... TIMEOUT !
BOOTP broadcast 1
BOOTP broadcast 2
BOOTP broadcast 3
BOOTP broadcast 4
This commit does not have an issue in itself, but it revelead a problem
with the Ethernet initialization.
As per the AR8035 datasheet:
"For a reliable power on reset, suggest to keep asserting the reset
low long enough (10ms) to ensure the clock is stable and clock-to-reset
1ms requirement is satisfied."
So do as suggested and keep the reset low for 10ms.
Also add a 100us delay after deasserting the reset line
to guarantee that the PHY ID can be read correctly and the Atheros
PHY can be loaded as per Troy Kisky's suggestion.
Signed-off-by: Fabio Estevam <fabio.estevam@nxp.com>
Tested-by: Tom Rini <trini@konsulko.com>
|
|\ \ |
|
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | | |
Various updates did not make it through to this board. Also the instructions
for building a SPI image are no-longer correct. Fix these so that Jerry can
boot to a prompt again.
Signed-off-by: Simon Glass <sjg@chromium.org>
|
| | |
| | |
| | |
| | |
| | |
| | | |
There is an unnecessary sector count displayed. Drop it.
Signed-off-by: Simon Glass <sjg@chromium.org>
|
| | |
| | |
| | |
| | |
| | |
| | | |
This feature was dropped at some point. Restore it.
Signed-off-by: Simon Glass <sjg@chromium.org>
|
|\ \ \
| | |/
| |/| |
|
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | | |
The problem is that timeout bits in WCR register were leaved unchanged.
So previously set timeout value was applied and therefore 'reset'
command takes any value up to two minutes, depending on previous
watchdog settings, instead of minimal 0.5 seconds.
Signed-off-by: Andrey Skvortsov <andrej.skvortzov@gmail.com>
|
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | | |
Override the default name_to_gpio() function with one that
accepts strings of the form bank:pin. If a colon is present
in the provided name, it behaves like the default version.
This lets the "gpio" command work with sane names rather than
requiring the user to enter the bank/pin composite in decimal.
Signed-off-by: Mans Rullgard <mans@mansr.com>
Reviewed-by: Stefano Babic <sbabic@denx.de>
|
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | | |
To TO1.0, we can not rely on finish bit to read temperature. But to
TO1.1, the issue was fixed by IC, we can rely on finish bit for
temperature reading for TO1.1.
Signed-off-by: Peng Fan <peng.fan@nxp.com>
Cc: Stefano Babic <sbabic@denx.de>
Cc: Tim Harvey <tharvey@gateworks.com>
Cc: Fabio Estevam <fabio.estevam@freescale.com>
Cc: Adrian Alonso <aalonso@freescale.com>
|
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | | |
With DEBUG macro enabled, SPL build failure:
"
arch/arm/cpu/armv7/built-in.o: In function `reset_misc':
~/uboot/arch/arm/cpu/armv7/mx6/soc.c:406: undefined reference to `lcdif_power_down'
scripts/Makefile.spl:244: recipe for target 'spl/u-boot-spl' failed
"
Wrap VIDEO settings with ifndef CONFIG_SPL_BUILD
Signed-off-by: Peng Fan <peng.fan@nxp.com>
Cc: Stefano Babic <sbabic@denx.de>
Reviewed-by: Stefano Babic <sbabic@denx.de>
|
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | | |
According to the Coverity result, a unsigned int variable is used fo less-
than-zero comparison, the result is never true. Need to fix the variable
type to signed int.
Signed-off-by: Ye.Li <B37916@freescale.com>
Signed-off-by: Peng Fan <peng.fan@nxp.com>
Cc: Przemyslaw Marczak <p.marczak@samsung.com>
Cc: Stefano Babic <sbabic@denx.de>
Reviewed-by: Stefano Babic <sbabic@denx.de>
|
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | | |
As per the AR8031 datasheet:
"For a reliable power on reset, suggest to keep asserting the reset
low long enough (10ms) to ensure the clock is stable and clock-to-reset
1ms requirement is satisfied."
So do as suggested and also add a 100us delay after deasserting the
reset line to guarantee that the PHY ID can be read correctly and the
Atheros 8031 PHY driver can be loaded automatically.
This results in a simpler code.
Signed-off-by: Fabio Estevam <fabio.estevam@nxp.com>
Acked-by: Joe Hershberger <joe.hershberger@ni.com>
|
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | | |
As per the AR8031 datasheet:
"For a reliable power on reset, suggest to keep asserting the reset
low long enough (10ms) to ensure the clock is stable and clock-to-reset
1ms requirement is satisfied."
So do as suggested and also add a 100us delay after deasserting the
reset line to guarantee that the PHY ID can be read correctly and the
Atheros 8031 PHY driver can be loaded automatically.
This results in a simpler code.
Signed-off-by: Fabio Estevam <fabio.estevam@nxp.com>
Acked-by: Joe Hershberger <joe.hershberger@ni.com>
|
| |/
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| | |
Commit 08ad9b068afb88 (" ar8031: modify the config func of ar8031 to
ar8021_config") selected 'ar8021_config' as the configuration function
for AR8031.
The correct would be to use 'ar8035_config' instead as AR8031/AR8035
have the same programming model and even share the same phy driver
in the linux kernel: drivers/net/phy/at803x.c.
Tested on a mx6qsabresd and wandboard, which now can work without
any PHY setup code in the board files.
Signed-off-by: Fabio Estevam <fabio.estevam@nxp.com>
Acked-by: Joe Hershberger <joe.hershberger@ni.com>
|
| |
| |
| |
| |
| |
| |
| |
| |
| | |
When trying to access non-existent/unsupported PCI devices in
ls_pcie_read_config(), when ls_pcie_addr_valid() fails it returns
error code and fills in the result with 0xffffffff manually. But it
really should return zero to upper layer codes.
Signed-off-by: Bin Meng <bmeng.cn@gmail.com>
|
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| | |
When trying to access non-existent/unsupported PCI devices in
imx_pcie_read_config(), when imx_pcie_addr_valid() fails it returns
error code and fills in the result with 0xffffffff manually. But it
really should return zero to upper layer codes.
Reported-by: Fabio Estevam <fabio.estevam@nxp.com>
Signed-off-by: Bin Meng <bmeng.cn@gmail.com>
Tested-by: Fabio Estevam <fabio.estevam@nxp.com>
|
| |
| |
| |
| | |
Signed-off-by: David Müller <d.mueller@elsoft.ch>
|
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| | |
from linux commit ce8155f7a3d5:
Perl 5.22 emits a deprecated message when "\C" is used in a regex. Perl
5.24 will disallow it altogether.
Fix it by using [A-Z] instead of \C.
>From linux adapted to U-Boot by:
Signed-off-by: Heiko Schocher <hs@denx.de>
Reviewed-by: Andre Przywara <andre.przywara@arm.com>
|
| |
| |
| |
| |
| |
| |
| |
| |
| | |
Since 51209b1f42cb ("Use common mtest iteration counting"),
do_mem_mtest has always reported 0 errors and hence returned 0, even
if errors were detected. Fix the helpers mem_test_alt() and
mem_test_quick() to return the number of errors found.
Signed-off-by: Rasmus Villemoes <rasmus.villemoes@prevas.dk>
|
| |
| |
| |
| |
| |
| |
| |
| | |
If CONFIG_SYS_STDIO_DEREGISTER is not enabled, usb reset
will fail every time. Enabling it allows usb reset to
work.
Signed-off-by: Andy Fleming <afleming@gmail.com>
|
| |
| |
| |
| |
| |
| | |
Change from yorksun@freescale.com to york.sun@nxp.com.
Signed-off-by: York Sun <york.sun@nxp.com>
|
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| | |
On these platforms we have many cases of boards that enable device model
and GPIO support but do not enable OF_CONTROL and pass in a device tree
with the binary. We need to bring in the platform data here as well.
Tested on Beaglebone Black.
Reported-by: Robert Nelson <robertcnelson@gmail.com>
Reported-by: Francisco Aguerre <franciscoaguerre@gmail.com>
Reported-by: Jason Kridner <jkridner@beagleboard.org>
Signed-off-by: Tom Rini <trini@konsulko.com>
|
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| | |
Mark _debug_uart_init() as static to avoid sparse warning and
inline it to debug_uart_init().
Reported-by: Thomas Chou <thomas@wytron.com.tw>
Signed-off-by: Michal Simek <michal.simek@xilinx.com>
Reviewed-by: Thomas Chou <thomas@wytron.com.tw>
Reviewed-by: Simon Glass <sjg@chromium.org>
Reviewed-by: Bin Meng <bmeng.cn@gmail.com>
Acked-by: Simon Glass <sjg@chromium.org>
|
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| | |
In many parts of the computing world having a unique MAC address
sitting in some on-NIC storage is considered the normal case.
Remove the warning to not scare the user unnecessarily.
This applies to Highbank/Midway and ARM's Juno, for instance.
Besides that this fixes the formatting on Midway, for instance,
which currently looks like:
...
Net: xgmac0
Warning: xgmac0 using MAC address from net device
, xgmac1
Warning: xgmac1 using MAC address from net device
...
Signed-off-by: Andre Przywara <andre.przywara@arm.com>
|
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| | |
The default kernel load offset for an arm64 kernel is 0x80000, so
U-Boot takes cares of moving the loaded kernel to a matching memory
location just before booting it.
Since we run with caches off, this takes a while for any decently
sized kernel - with no output explaining the reason for the delay
(unless one uses a DEBUG build).
By adjusting the default load offset for Juno and VFP to be 512K
aligned in the first place we can skip this copying and boot much
faster.
Tested on Juno.
Signed-off-by: Andre Przywara <andre.przywara@arm.com>
Reviewed-by: Linus Walleij <linus.walleij@linaro.org>
Tested-by: Ryan Harkin <ryan.harkin@linaro.org>
|
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| | |
The compilation of u-boot-dtb.img should be controlled by
CONFIG_OF_CONTROL and not CONFIG_DM.
CONFIG_DM may be defined even without Device Tree requirement.
This was added in commit 947cee1127c5fa97529c8cda4f0b48d141f92560.
Signed-off-by: Ruchika Gupta <ruchika.gupta@freescale.com>
Signed-off-by: Aneesh Bansal <aneesh.bansal@freescale.com>
CC: Alison Wang <alison.wang@freescale.com>
|
| |
| |
| |
| |
| |
| |
| |
| |
| | |
Correct mismatched comment on #endif to agree with its #if defined().
Also add some missing #endif comments for consistency, take out
extraneous blank lines for readability.
rday
|
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| | |
First (small) pass at tidying up the README file, including:
* remove references to obsolete CREDITS file
* remove (some) references to obsolete boards.cfg file
* remove at least one reference to a "scrapped" board
* cut down unnecessarily detailed directory hierarchy
* bunch of grammar and spelling tweaks
Signed-off-by: Robert P. J. Day <rpjday@crashcourse.ca>
|
| |
| |
| |
| | |
Signed-off-by: Robert P. J. Day <rpjday@crashcourse.ca>
|
| |
| |
| |
| |
| | |
Signed-off-by: Robert P. J. Day <rpjday@crashcourse.ca>
Acked-by: Thomas Chou <thomas@wytron.com.tw>
|
|\ \ |
|
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | | |
Introduced in 45b4773 (net/arp: account for ARP delay, avoid duplicate packets on timeout)
Check the arp timeout and adjust the timeout start time before the call
to eth_recv() so that the sandbox driver has the opportunity to adjust
the sandbox timer after the new start time has been recorded.
Also, change the adjustment amount by 11 seconds instead of exactly the
10 seconds that the ping timout is expecting since the timeout check is
looking for the time elapsed to be greater than but not equal to the
specified delay.
Signed-off-by: Joe Hershberger <joe.hershberger@ni.com>
Reviewed-by: Stefan Brüns <stefan.bruens@rwth-aachen.de>
Acked-by: Simon Glass <sjg@chromium.org>
|
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | | |
Commit: dm: core: Enable optional use of fdt_translate_address()
Enables use of this function as default, but after this it's not
possible to get dev address for the case in which: '#size-cells == 0'
This causes errors when getting address for some GPIOs, for which
the '#size-cells' is set to 0.
Example error:
'__of_translate_address: Bad cell count for gpx0'
Allowing for that case by modifying the macro 'OF_CHECK_COUNTS',
(called from )__of_translate_address(), fixes the issue.
Now, this macro doesn't check, that '#size-cells' is greater than 0.
This is possible from the specification point of view, but I'm not sure
that it doesn't introduce a regression for other configs.
Please test and share the results.
Tested-on: Odroid U3, Odroid X2, Odroid XU3, Sandbox.
Signed-off-by: Przemyslaw Marczak <p.marczak@samsung.com>
Cc: Masahiro Yamada <yamada.masahiro@socionext.com>
Cc: Lukasz Majewski <l.majewski@samsung.com>
Cc: Jaehoon Chung <jh80.chung@samsung.com>
Cc: Stefan Roese <sr@denx.de>
Cc: Simon Glass <sjg@chromium.org>
Cc: Bin Meng <bmeng.cn@gmail.com>
Cc: Marek Vasut <marex@denx.de>
Tested-by: Jaehoon Chung <jh80.chung@samsung.com>
Tested-by: Lukasz Majewski <l.majewski@samsung.com>
|
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | | |
At present USB keyboards are not properly removed with driver model. Add the
code to handle this.
Signed-off-by: Simon Glass <sjg@chromium.org>
Reviewed-by: Marek Vasut <marex@denx.de>
|
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | | |
The current limit of 5 is not enough for the driver model USB tests. Really
we should not have a limit but the driver model code still uses the
usb_dev_desc[] array, which has a limit.
Increasing the limit by 2 should not bother anyone. Adjust it.
Signed-off-by: Simon Glass <sjg@chromium.org>
Reviewed-by: Marek Vasut <marex@denx.de>
|
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | | |
This subsystem has been broken since commit:
4efad20a sf: Update status reg check in spi_flash_cmd_wait_ready
There has so far been no response from the maintainer, and a release is
imminent. For now, let's just disable the tests.
Signed-off-by: Simon Glass <sjg@chromium.org>
|
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | | |
When 'ethrotate' variable is set to 'no' and 'ethact' variable
is already set to an ethernet device, we should stick to 'ethact'.
Signed-off-by: Bin Meng <bmeng.cn@gmail.com>
Acked-by: Joe Hershberger <joe.hershberger@ni.com>
Acked-by: Simon Glass <sjg@chromium.org>
Tested-by: Simon Glass <sjg@chromium.org>
|
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | |
| | | |
In eth_current_changed(), the call to eth_get_dev() below has a side
effect of rotating ethernet device if uc_priv->current == NULL. This
is not what we want when 'ethrotate' variable is 'no'.
Signed-off-by: Bin Meng <bmeng.cn@gmail.com>
Acked-by: Joe Hershberger <joe.hershberger@ni.com>
Acked-by: Simon Glass <sjg@chromium.org>
Tested-by: Simon Glass <sjg@chromium.org>
|
| |/
| |
| |
| |
| |
| |
| |
| | |
Add missing sandbox timer to test.dts, so that test-dm works.
Signed-off-by: Thomas Chou <thomas@wytron.com.tw>
Acked-by: Simon Glass <sjg@chromium.org>
Tested-by: Simon Glass <sjg@chromium.org>
|
|\ \
| |/
|/| |
|
| |
| |
| |
| |
| |
| |
| |
| |
| | |
This commit fixes the change of below commit
"spi: fsl_qspi: Use GENMASK"
(sha1 :bad490a24212c068c5b718b9189f47ea4075d078)
Signed-off-by: Gong Qianyu <Qianyu.Gong@freescale.com>
Reviewed-by: Jagan Teki <jteki@openedev.com>
|
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| | |
stm_is_locked_sr() takes the status register (SR) value as the last
parameter, not the second.
Based on a patch from Brian Norris for the linux kernel:
http://git.infradead.org/linux-mtd.git/commit/a32d5b726ff8cf32bf491522b0ac8ae2545a063e
Signed-off-by: Fabio Estevam <fabio.estevam@nxp.com>
Reviewed-by: Jagan Teki <jteki@openedev.com>
|
|\ \ |
|
| |/
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| | |
since:
commit: f05ad9ba "Add a way to skip relocation"
tqm5200s board fails to boot. Reason is that
board_init_f has a function parameter bootflag,
which is not setup in
in arch/powerpc/cpu/mpc5xxx/start.S _start
So board_init_f gets a undefined bootflag,
currently the gd pointer address. Unfortunately
this address sets the GD_FLG_SKIP_RELOC bit,
so u-boot code gets not relocated and u-boot
does not boot ...
Init bootflag with 0, and tqm5200 boots fine again.
Signed-off-by: Heiko Schocher <hs@denx.de>
Reviewed-by: Simon Glass <sjg@chromium.org>
Reviewed-by: York Sun <yorksun@freescale.com>
|
| |
| |
| |
| | |
Signed-off-by: Tom Rini <trini@konsulko.com>
|
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| | |
Use snprintf to replace sprintf.
Coverity log:
"
Unbounded source buffer (STRING_SIZE)
string_size: Passing string init_val of unknown size to sprintf.
"
Reported-by: Coverity
Signed-off-by: Peng Fan <peng.fan@nxp.com>
Cc: Tom Rini <trini@konsulko.com>
Cc: Simon Glass <sjg@chromium.org>
Reviewed-by: Joe Hershberger <joe.hershberger@ni.com>
|
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| |
| | |
Before calling hsearch_r, initialize callback entry to NULL.
Coverity log:
"
Uninitialized scalar variable (UNINIT)
uninit_use_in_call: Using uninitialized value e.
Field e.callback is uninitialized when calling hsearch_r.
"
Reported-by: Coverity
Signed-off-by: Peng Fan <peng.fan@nxp.com>
Cc: Tom Rini <trini@konsulko.com>
Cc: Simon Glass <sjg@chromium.org>
|